Board Layout Recommendation to Improve
Transient Response
Internal Current Limit
Shutdown
(Fixed Voltage Versio n)
dVdt VOUT
COUT 80kRLOAD
(4)
Dropout Voltage
(Adjustable Voltage Version)
dVdt VOUT
COUT 80k(R1R2)RLOAD
(5)
TPS736xx
SBVS038K – SEPTEMBER 2003 – REVISED SEPTEMBER 2005
This noise reduction effect is shown as RMS Noise For large step changes in load current, the TPS736xxVoltage vs C
NR
in the Typical Characteristics section. requires a larger voltage drop from V
IN
to V
OUT
toavoid degraded transient response. The boundary ofThe TPS73601 adjustable version does not have the
this transient dropout region is approximately twicenoise-reduction pin available. However, connecting a
the dc dropout. Values of V
IN
- V
OUT
above this linefeedback capacitor, C
FB
, from the output to the FB
insure normal transient response.pin will reduce output noise and improve load transi-ent performance. Operating in the transient dropout region can causean increase in recovery time. The time required toThe TPS736xx uses an internal charge pump to
recover from a load transient is a function of thedevelop an internal supply voltage sufficient to drive
magnitude of the change in load current rate, the ratethe gate of the NMOS pass element above V
OUT
. The
of change in load current, and the available head-charge pump generates ~250µV of switching noise at
room (V
IN
to V
OUT
voltage drop). Under worst-case~4MHz; however, charge-pump noise contribution is
conditions [full-scale instantaneous load change withnegligible at the output of the regulator for most
(V
IN
- V
OUT
) close to dc dropout levels], the TPS736xxvalues of I
OUT
and C
OUT
.
can take a couple of hundred microseconds to returnto the specified regulation accuracy.
PSRR and Noise PerformanceTo improve ac performance such as PSRR, output
The low open-loop output impedance provided by thenoise, and transient response, it is recommended that
NMOS pass element in a voltage follower configur-the board be designed with separate ground planes
ation allows operation without an output capacitor forfor V
IN
and V
OUT
, with each ground plane connected
many applications. As with any regulator, the additiononly at the GND pin of the device. In addition, the
of a capacitor (nominal value 1µF) from the output pinground connection for the bypass capacitor should
to ground will reduce undershoot magnitude butconnect directly to the GND pin of the device.
increase duration. In the adjustable version, theaddition of a capacitor, C
FB
, from the output to theadjust pin will also improve the transient response.The TPS736xx internal current limit helps protect the
The TPS736xx does not have active pull-down whenregulator during fault conditions. Foldback helps to
the output is over-voltage. This allows applicationsprotect the regulator from damage during output
that connect higher voltage sources, such as alter-short-circuit conditions by reducing current limit when
nate power supplies, to the output. This also resultsV
OUT
drops below 0.5V. See Figure 11 in the Typical
in an output overshoot of several percent if loadCharacteristics section for a graph of I
OUT
vs V
OUT
.
current quickly drops to zero when a capacitor isconnected to the output. The duration of overshootcan be reduced by adding a load resistor. Theovershoot decays at a rate determined by outputThe Enable pin is active high and is compatible with
capacitor C
OUT
and the internal/external load resist-standard TTL-CMOS levels. V
EN
below 0.5V (max)
ance. The rate of decay is given by:turns the regulator off and drops the ground pincurrent to approximately 10nA. When shutdown capa-bility is not required, the Enable pin can be connectedto V
IN
. When a pull-up resistor is used, and operationdown to 1.8V is required, use pull-up resistor valuesbelow 50k Ω.
The TPS736xx uses an NMOS pass transistor toachieve extremely low dropout. When (V
IN
- V
OUT
) isless than the dropout voltage (V
DO
), the NMOS passdevice is in its linear region of operation and theinput-to-output resistance is the R
DS-ON
of the NMOSpass element.
12